56mm Throttle body
- Victor Meldrew
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56mm Throttle body
Well its fitted.
Not totaly problem free but its running.
My God its quick.
The car used to run out of puff after 6000 rpm but it now pull strong right to the limiter. .
Will post a few pics later.
Not totaly problem free but its running.
My God its quick.
The car used to run out of puff after 6000 rpm but it now pull strong right to the limiter. .
Will post a few pics later.
Well it moves... might as well make the most of it....
- Victor Meldrew
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Last edited by Victor Meldrew on Fri Aug 18, 2006 8:57 pm, edited 1 time in total.
Well it moves... might as well make the most of it....
- Victor Meldrew
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In this pic you can see the small bore breather hose, (the white one) that goes roughly where the original hose should be. I drilled a 4mm hole through the un-finnished moulding spar and mounted the hose onto that.
I was thinking about fitting an oil catch tank and seperate breather... I dont know if the small hole is big enough...
I was thinking about fitting an oil catch tank and seperate breather... I dont know if the small hole is big enough...
Last edited by Victor Meldrew on Fri Aug 18, 2006 8:59 pm, edited 1 time in total.
Well it moves... might as well make the most of it....
Just keep and eye on it and see what happens. Probably not worth it. If it looks like it is clagging up then enlarge the hole. Catch tank will just soot up eventually anyway if the hole's not big enough.
1994 Lotus Esprit S4 - Work in progress
1980 Porsche 924 Turbo - Funky Interior Spec
2004 Smart Roadster Coupe - Hers
1980 Porsche 924 Turbo - Funky Interior Spec
2004 Smart Roadster Coupe - Hers
- Victor Meldrew
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if you look at the throttle body in this pic you can see there has been part of the casting taken off and a hole drilled and tapped for the idle adjuster screw. I dont know what was here originaly as it was modified by the bloke I bought it off.
The other problem is the actuator cam that the cable goes to, it isnt the same profile as the std cam. I needed another inch of throttle pedal travel to get full open on the new throttle body. It was a quick easy fix by adjusting the throttle end stop under the pedal. The original cam may fit but I havnt had time to play around with it, still building the garden shed. I have the upgrade throttle lever pivot kit (pedal box) fitted which gives three pick up points for the throttle tie bar, I should be able to get full open with the original pedal travel if I spend time messing around with this.
I havnt found the extra travel to be a problem, if anything it is easier to balance throttle mid corner as you dont need to be so fine with your adjustments.
The other problem is the actuator cam that the cable goes to, it isnt the same profile as the std cam. I needed another inch of throttle pedal travel to get full open on the new throttle body. It was a quick easy fix by adjusting the throttle end stop under the pedal. The original cam may fit but I havnt had time to play around with it, still building the garden shed. I have the upgrade throttle lever pivot kit (pedal box) fitted which gives three pick up points for the throttle tie bar, I should be able to get full open with the original pedal travel if I spend time messing around with this.
I havnt found the extra travel to be a problem, if anything it is easier to balance throttle mid corner as you dont need to be so fine with your adjustments.
Last edited by Victor Meldrew on Fri Aug 18, 2006 9:00 pm, edited 1 time in total.
Well it moves... might as well make the most of it....
- craigs135s
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- Location: Edinburgh
- Victor Meldrew
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fleebay, and here is another two.craigs135s wrote:John where did you get the 56 TB and how did it cost if you dont mind me asking???
Cheers
Craig
http://cgi.ebay.co.uk/56mm-THROTTLE-BOD ... otohosting
http://cgi.ebay.co.uk/rover-k-series-el ... dZViewItem
Last edited by Victor Meldrew on Tue Aug 08, 2006 12:58 am, edited 1 time in total.
Well it moves... might as well make the most of it....
- Victor Meldrew
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- craigs135s
- Posts: 1960
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- Location: Edinburgh
- Victor Meldrew
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I just had the std plastic one which was sticking like a really sticky thing, which was my main motivation for changing it. When I found these 56mm jobs going for pennies I thought, might as well try it. Better than giving elise parts £140 notes...craigs135s wrote:cool john can you let me no???Did you have a 52 before the 56?or just the standerd?
Cheers
Craig
As you can see I have a coolflow induction kit on it as well. The two combined make a very noticable difference, especialy at higher revs.
Well it moves... might as well make the most of it....
- Victor Meldrew
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I assume your talking about the oil filler cap. The air filter housing is chromed plastic.GregR wrote:loving the ali tat too John
I too have el coolflow, but ripped off the tumble-tryer ducting as it was rattling too much. Have you had to clean yours yet?
Oh, I have an ally 52mm TB btw
Not had to clean it yet but I have the K&N oil and cleaner stuff that I use on my S6. When it was out for the throttle fitting it looked Ok. Only had it on for a few thousand miles. The whole point of the coolflow is the ducting, your just pulling hot air in from the engine bay. Not good.
Well it moves... might as well make the most of it....